Success with new toy!
Posted: Sun Feb 01, 2015 4:36 pm
I got a new Lincoln Weld-Pak 140HD a couple weeks ago. It had been eight years since welding anything, so I was anxious to give it a try. I had some 1/8" x 1" HRS left over from a project long ago. I cut a few 6" pieces and cleaned them up a bit with a wire wheel on the bench grinder. They were relatively clean, but not shiny. I didn't have a good table to weld on, so I clamped a piece of 1/2" x 2" CRS (very clean) in a B&D workmate, clamped the workpiece and ground cable to opposite ends, and started practicing. I was using .035" NR-211-MP at the setting recommended on the chart inside the welder door, and got terrible results. There was a lot of splatter and porosity. The weld bead was nearly flush with the top surface and the opposite side of the workpiece had a heavy bead of weld protruding out. I wondered if the recommended settings were off that much or if my technique was at fault. I had watched lots of Jody's videos and kept trying different things with my technique, leaving the settings on the welder alone. Yes, the polarity was correct. I was plugged into a 15A circuit that was also powering a small fluorescent light and three battery tenders in float mode. The breaker tripped once while welding.
I have since installed a separate 20A outlet just for the welder, and it's very close to the service panel. I picked up more 1/8" x 1" HRS from the hardware store. This time the pieces were cleaned up nice and shiny with a flap sanding disc. Yesterday I brought home one of Harbor Freight's adjustable welding tables. It's pretty decent for the price. Today, my results were just about perfect. I started with lower settings, but had all the symptoms of being set too low. Returning to the recommended settings, and making small adjustments to my travel speed, yielded some very nice looking welds.
So, I broke my own rule of troubleshooting and changed three variables (new outlet, new table, new material). I'd like to blame the old material, or it's lack of proper preparation, but maybe powering the welder on its own circuit had something to do with it. I doubt the table had anything to due with the issue, but it sure is nice and handy. Regardless of the previous frustration or today's success, I'm pleased with my new toy and just wanted to share.
I have since installed a separate 20A outlet just for the welder, and it's very close to the service panel. I picked up more 1/8" x 1" HRS from the hardware store. This time the pieces were cleaned up nice and shiny with a flap sanding disc. Yesterday I brought home one of Harbor Freight's adjustable welding tables. It's pretty decent for the price. Today, my results were just about perfect. I started with lower settings, but had all the symptoms of being set too low. Returning to the recommended settings, and making small adjustments to my travel speed, yielded some very nice looking welds.
So, I broke my own rule of troubleshooting and changed three variables (new outlet, new table, new material). I'd like to blame the old material, or it's lack of proper preparation, but maybe powering the welder on its own circuit had something to do with it. I doubt the table had anything to due with the issue, but it sure is nice and handy. Regardless of the previous frustration or today's success, I'm pleased with my new toy and just wanted to share.